Soilworks products are the industry’s top standard due to our insistence on creating high performance soil stabilization and dust control products that stand up to rigorous testing – both in the lab and in the field. Our commitment to quality and performance has led to our involvement and testing in hundreds of real-world situations. The following library of reports, presentations, specifications, approvals and other similar documents provide you, our customer, the transparency and dependable assurance that is expected from Soilworks.
PART 1.4- FINDINGS
METHODOLOGY
Model of Detailing Factors. In determining the causal and other factors that led to the accident, the Panel detailed each area broadly following Reason ‘s ‘Swiss Cheese’ model1, which divides the factors leading to the accident into the following 4 areas:
Accident Factors . Each factor that was attributed to Reason ‘s model was then detailed in accordance with JSP551 as one of the following:
Available Evidence.The SI Panel had access to a significant amount of evidence, which enabled a thorough investigation into all possible factors concerning the accident and left very few areas of uncertainty. Evidence included:
Unavailable Evidence. The Panel did not have access to the following:
Services. To assist the Panel, the services of the following personnel and agencies were made available:
Factors Not Considered. The Panel was unable to fulfil the requirement in the TORs to assess the environmental implications relating to the accident. The Panel noted that the pressures to expediently recover the ac resulted in fuel and material, including engines and composite blades remaining at the site for destruction. The Panel did not have access to the final landing site.
ORGANISATIONAL INFLUENCES
Operational Context. Helicopter operations in Afghanistan are flown against a high insurgent threat, often at the edge of the aircraft and aircrew operating capability, and in the face of significant operational pressures to support those forces that are at even greater risk on the ground. In the year prior to the ZA708 accident, the number of ground forces in the Helmand AO increased and the number of established HLSs rose from approximately 20 to around 100. As part of the ‘clear, hold and build’ strategy, many of these HLSs were adjacent to populated areas and thus faced an increased threat. Despite the threats and other risks to aviation, the use of helicopters still represented the ‘least bad’ option when compared with road resupply, which was vulnerable to IED and other attacks. The increased threat to aviation was often mitigated by ac operating at night , which in itself increases the risk to crews by the greater difficulty of the flying task – crews operate with a restricted field of view and reduced depth perception during NVD operations. The combination of threat, environmental and other demands found in Afghanistan result in JHC aircraft operating with a level of risk that is higher than in other recent theatres of operation. This is borne out by data provided by HQ JHC detailing dust-related incidents in the year prior to ZA708 ‘s accident, many of which were attributed to the ‘natural operating hazards’ of the theatre (Fig 1-9). The Panel concluded that the demanding environmental nature of Afghan operation s was a contributory factor to theaccident.
Figure 1-9 JHC data detailing significant dust incidents in the year prior to the ZA708 accident
HLS Management.
Fig 1-10 Computer model ‘plan’ view of CH47 in PB Bahadur HLS (with FP wall built)
The Panel concluded that the lack of robust HLS management was a major contributory factor to· the accident.
SUPERVISION
HLS FACTORS
The Panel concluded that the omission to notify JHF(A) of the FP measures that reduced the HLS size was a major contributory factor to the accident.
Fig 1-11 The construction of a new FP wall and the impact point of the CH47 on the pre-existing wall
HLS Dust Suppression Measures. Dust suppression is achieved in Theatre through the laying of aggregate , AM2 dust suppression matting, Durasoil (a clear synthetic organic fluid which is sprayed onto the site, binding with dust particles to produce a dust suppressing barrier) or a combination of the above. PB Bahadur was identified by JHF(A) as requiring dust suppression on or before 8 May 10. On 28 May 10, a Statement of Requirement (SoR) for the dust suppression of the site was passed to Joint Force Support (Afghanistan) (JFSp(A)) by JHF(A). After negotiation with JFSp(A), who had stated that such an SoR should come from the HLS owner, JHF(A) resubmitted a SoR for the dust suppression of both PB Nahidullah and Bahadur on 6 Jun 10. Nahidullah had been incorporated due to the tact that on 2 Jun 10, a Merlin crew had raised a flight safety concern regarding the dust at the HLS. The Panel found that the meaning of HLS ‘owner’ was poorly defined, with some witnesses thinking it was the MAOT and some thinking it was the user unit. The only definition found was that of an ‘HLZ Manager’, which in the Headquarters Regional Command (South) SOP 3706, was defined as ‘a suitably experienced/ qualified soldier nominated from the user unit. On 19 Jun 10, JHF(A) submitted a report to JFSp(A) citing the potential for loss of life if the requested HLS dust suppression work was not afforded adequate priority. Due to the limited engineering resources in Afghanistan, on 21 Jun 10 COMJAG requested for CO JHF(A) to provide a list of the 1O HLS at which crews encountered the worst brown-out conditions. This information would be used to prioritise HLS dust suppression engineering works. The ‘Top Ten’ priority list for dust suppression, produced by JHF(A), originally listed PB Nahidullah and PB Bahadur as the worst and second worst HLSs respectively. On 23 Jun 10, shortly after this list was compiled and on the same day that dust suppression was discussed and not approved at an informal meeting in TFH, Merlin (S26) crashed while approaching PB Nahidullah HLS. Brown-out and un-notified ground engineer work were cited as contributory factors to the accident. Dust suppression measures were subsequently put in place at PB Nahidullah on 28 Jun 10.
Impact of FP Measures on Dust in HLS.The Panel found that the construction of the new FP wall at PB Bahadur was achieved by the frequent and regular movement of armoured plant machinery heavy vehicles (Fig 1-12a) over and across the HLS between 5 and 9 Aug 1O. The weight and non- pneumatic tyre design of this vehicle served to break up the surface of the HLS and transform it from compressed mud and sand into talcum-powder like dust. The Panel found that while existing HLS management procedures in Theatre prohibited the use of vehicles on a HLS in wet weather, they were not clear about dry weather. In the case of Bahadur, the only entrance to the Bahadur PB compound was across the HLS itself and constant movement of vehicles across the HLS would have served to further exacerbate this situation. The Panel consider that the effect of this work was to significantly increase the levels of dust on the HLS (Fig 1-12b), which was unsuppressed (i.e. no matting or gravel); this dust was described as ankle deep by a MAOT officer during a visit to the HLS over the period 18-19 Aug 10, a week after the accident. ZA708 was the first aircraft to approach this HLS after the FP work was completed and, tasked with the carriage of an USL, would have been exposed to the dust for a significant period of time. The Panel concluded that the omission to notify JHF(A) of the unsupressed and excessive dust as a result of the FP work on the HLS and mitigate against its presence was a major contributory factor to the accident.
Fig 1-12a Type of vehicle used for FP work
Fig 1-12b Excessive dust (note footprints)
SUPERVISION OF FLYING
Supervision of the HP by the Crew of ZA708 – Cockpit Gradient. The SI Panel analysed the full hour of cockpit voice recorded prior to the accident, which covers all but the first 10 minutes of the sortie. The crew conversations throughout the sortie are of a professional nature, with no indications of poor working relationships or clashes of personality. However, during the Panel’s interviews of the NHP, No 1 and No 2 crewman, it was discovered that the HP’s flying abilities were held in high regard by his crew. This was possibly due to his standing within the Chinook Wing as a previous Sqn Standards Officer (StanO) and Chinook Display Pilot and the flying ability associated with these positions. There was evidence that the HP had previously flown non-standard profiles but, due to his experience and handling skills, these profiles had been accepted and not questioned by his crew. (S41) other aircrew on the detachment. However, he was additionally faced with the supervisory responsibilities of a flt cdr, including ensuring JHF(A) tasking was appropriate. The Panel found that Chinook tasking from JHF(A) was very demanding, requiring frequent changes of aircrew shift patterns that occurred without full consideration of the cumulative impact on the flt. The Panel found some members of 1310 Flt – but none of the crew of ZA708 – had resorted to the prescribed use of Temazepam to overcome the frequent changes in sleep patterns (covered further in para 18). The Panel found evidence of one occasion where an ac captain had declared himself unfit to fly for a training sortie due to fatigue but had been persuaded by OC 131O Flt to conduct the sortie regardless. Further, the crew of ZA708 comments to the HFP included:
(S41)
In contrast, the Panel interviewed the previous and subsequent QC 131O Fits and found that both deployed as an additional crew member, outside of the constituted crew system, in order to have the flexibility to balance the flying against the wider managerial, supervisory and leadership challenges of the role. Both stated that this system, combined with their previous experience from a ground tour as a sqn ldr, allowed them greater opportunities to influence, adjust – and if required reject – tasking at an early stage. As such, they did not assess the fatigue issues as being as significant, they did not personally or collectively conduct the same high level of flying and, to their knowledge, their crews were not using Temazepam. Further, the Panel interviewed the detachment commanders of the other aircraft types at JHF(A), with none reporting fatigue as a significant factor. Consequently, the Panel concluded that while not an endemic, force-wide problem across detachments , there was a cultural shift from ‘Can-do- safely to ‘ Can-do’ on this detachment that was not addressed due to the high workload on QC 131O Flt as part of his role in a constituted crew. The Panel concluded that the lack of robust fatigue management and supervision of 131O Flt was a contributory factor in the accident.
The Use of Temazepam. The Panel found that some 1310 Flt aircrew had resorted to the prescribed use of Temazepam to maximise the amount of sleep they could get during their erratic and often short-notice crew rest periods. When questioned, all members of the crew of ZA708 stated that they had not taken the drug during the days leading up to this mission. (S41)
. The Panel found that those members of 131O Flt who used Tamazepam and the medical personnel who prescribed them did so at variance to the regulations specified for its use in JSP 550.
Specifically, they did not inform their chain of command before taking it. When interviewed about this subject, CQMJAG, CO JHF(A) and QC 1310 Flt all expressed surprise and concern that their aircrew were using this drug without their knowledge. Whilst not a contributory factor for this SI, the Panel found cause for concern that the treatment of fatigue was an in-Theatre issue only for the Chinook crews and that the COMJAG/JHF(A) command chain had no knowledge of the use of Temazepam by some aircrew. The Panel concluded that the use of Temazepam was not a contributory factor in this accident
Supervision of OC 1310 Flt (HP). The HP had only recently been promoted to sqn ldr and, on his first detachment as OC 131O Fl t, was responsible for (S26) aircraft, (S26) crews, engineers and ground staff (all split between Kandahar and Bastion airfields) as well as being ac captain of one of the crews.
(S41)
The HP’s fatigue was noted by his sqn cdr during a weekly telephone conversation from the UK, with the sqn cdr commenting that the HP appeared tired; he reported sensing an improvement during their subsequent conversation. During his interview, CO JHF(A) stated that he regularly attended JMBs and sent individuals to bed that he thought were fatigued. Indeed, during his interview, the COS JHF(A) stated that the CO JHF(A) would lead by example on the issue of crew rest when he was flying and that he considered it a rule not to be broken. However, the Panel found that the evidence of fatigue on 1310 Flt and with OC 131O Flt in particular did not reflect this. The Panel noted an acceptance that the Chinook detachment would ‘run hot’, compared with other JHF(A) detachments , due to their shorter deployment periods and the significant cumulative fatigue of OC 1310 Flt was either not recognised or was not addressed in HQ JHF(A). (S41)
. The Panel concluded that the lack of robust supervision of OC 1310 Flt – the HP – in theatre was a contributory factor in the accident.
Supervision of JHF(A) . COMJAG was responsible for the direct supervision of JHF(A) and other UK aviation operations in Afghanistan. Geographically some distance away from the JHF(A) infrastructure in the (S27), he maintained a command overview of JHF(A) operations and coordinated the employment of JHF(A) assets within the (S27), but also dealt with TFH on a daily basis. His position was therefore more akin to a stn cdr than a sqn cdr; he ensured tasking apportionment was correct and appropriate, set direction for commanders and provided appropriate representation and reporting to higher formations. While COMJAG would speak with aircraft detachment commanders on arrival and would regularly engage with CO JHF(A), JHF(A) was responsible for day to day supervision and implementation of flying. The Panel found the JAG command chain had a high level of risk awareness. In terms of threat, there was a firm mission-orientated atmosphere within JAG and therefore an understandable and justifiable focus on a recent dramatic rise in SAFIRE events against UK aviation. For other risks, the Panel also found that COMJAG was strongly pursuing measures to increase aviation safety and minimise risk to aviation operations. For HLS management and dust suppression, there was compelling evidence of COMJAG and JHF(A)’s efforts to resolve this problem, activity that commenced before the Merlin accident of 23 Jun 10. However, interviews with DCOS TFH and CO 21 Eng Regt confirmed these requirements were balanced against other demands for engineering assistance, in particular measure to improve protection for ground elements. While evidence did show that COMJAG acted swiftly on all safety issues raised, the Panel could not find evidence that the creeping reduction in HLS size was ever raised to the COMJAG level. The Panel recognise that, with troops already on the ground, there may still have remained an operational imperative to support them until adjustments could be made. The Panel concluded that supervision of JHF(A) by COMJAG was not a factor in the accident.
PERSONNEL ON THE HLS
Sleeping Accommodation Adjacent to the HLS. There were 2 structures within the PB Bahadur compound; one was used as the Ops Room and the other as accommodation. Both buildings were of adobe-type construction and attached to the perimeter wall of the compound adjacent to the HLS. The accommodation building was located exactly where the fuselage of ZA708 struck the compound wall and due to its construction, led to the collapse of the roof. the serviceman involved in the accident was alone in the building because most of the PB personnel slept in the open at night. Due to the restricted size of the HLS and irrespective of the fact that the accident occurred, the Chinook’s rotor blades would have been overlapping the compound wall. The Panel questioned the efficacy of having non-duty personnel so close to flying operations, especially given the infrequent use of this HLS and the fragility of local constructions. In addition, the Panel has also found that ZA708 may have been in a state of dynamic rollover when, due to incredible fortune, the rear rotor struck the top of the sangar and the ac righted itself. Given the compound size, the Panel opined that if the ac had rolled into the compound there would have been significantly more danger to the PB personnel and a high risk of additional loss of life or serious injury, both to the crew and those within the compound. When interviewed, the CO of 21 Engr Regt stated that the arched roofs of these adobe-type buildings sometimes collapse under the weight of a gun position or even personnel walking on them. The 1 Mercian Learning Account recognised these points and, inter alia, recommended that all personnel should be in Personal Protective Equipment (PPE) for flying operations. Given the small size of the HLS, which increased the likelihood of an incident, the Panel found that having personnel accommodated within this building during flying operations was an unacceptable risk. The Panel found that the use of an ‘adobe’-type structure, adjacent to the HLS, for sleep during a helicopter insert was an aggravating factor in the accident.
Engines and Fuel System. A loss of engine power at a critical stage of the approach could have led to the HP having a reduced ability to control the height of the ac in close proximity to the PB compound wall. The SI Panel analysed crew interviews, IR video footage of the accident, engine data recorded by the CVFDR system, HUMS data and ZA708’s F700. CVFDR data showed that both engines were well matched and were performing normally. During the overshoot from. PB Bahadur, following the accident, Engine 1 and 2 achieved 119.75 % torque and 123.5 % torque respectively. This power output exceeds the estimated maximum power output of the engines (at the operating density altitude) obtained from the ac’s performance planning data. Both engine power turbine inlet temperatures (PTITs) remained within the specified transient power limits for the duration of the sortie, with the maximum temperature recorded being on Engine 2 at 914°C. HUMS data analysis has shown no excessive engine vibration levels or exceedances. The CVFDR data also shows that engine fuel flow was commensurate with the power being demanded by the HP. However, the ‘L FUEL PRESS’ (left fuel pressure) CAP caption illuminated for a duration of approximat y one second, one second after the initial collision with the compound wall. The Panel consider that this transient caption may have been the result of the sudden increase in demanded fuel flow, reducing the pressure in the engine HP pump supply line to value below the CAP caption trigger value of 1O p si, but there was no evidence to suggest that the fuel supply to either engine had been interrupted. No reference was made to any perceived or actual engine problems during crew interviews. There were several reports of smoke coming from Engine 1 after the impact from witnesses who observed the IR camera footage. The SI Panel has analysed the IR video camera footage of the accident. As the IR camera was set to ‘black hot’, the heat of the engine exhaust plume appeared as black smoke in the footage. The SI panel has concluded that the witnesses mistook this IR plume for smoke. Fuel and engine oil samples were taken and subsequently analysed. There were no unusual findings.
Automatic Flying Control System ( AFCS) . As the Chinook AFCS has a direct input to the roll, pitch and yaw channels of the ac flying controls, the possibility of an AFCS malfunction was investigated. Although there were no indications of any issue with this system, both AFCS computers were sent to RAF Odiham for testing. They were subsequently found to be serviceable, despite minor testing errors associated with barometric pressure changes resulting from their transportation from Afghanistan to the UK. The Chinook AFCS performs several functions relevant to the USL drop-off profile:
a. Heading Hold. (S26).
Annex A (Fig 6)
b. Pitch Attitude Hold. (S26).
Annex A (Fig 2)
c. Bank Angle Hold. (S26).
Annex A (Fig 1)
Flying Controls. Interviews with the crew and analysis of CVFDR and HUMS data indicated that the ac was responding correctly to flying control inputs. This data, combined with the extensive damage inflicted on the aft rotor during the accident, the expedient rotor blade removal process and the aerial recovery process (which involved lifting ZA708 by its rotor heads), led the Panel and RNFSAIC to conclude that a full flying control inspection was not required. Hydraulic oil samples were taken and subsequently analysed, with no unusual findings
Transmissions and Rotor System. There were no unusual transmission indications for the duration of the sortie. Although the HP reported seeing possible transmission-related CAP captions during the overshoot manoeuvre after the accident, there was no evidence of this in the CVFDR data. HUMS data has shown that there were no unusual vibrations from the airframe or transmissions prior to the accident. Photographic evidence has shown that the aft ‘green’ rotor lag damper had detached from the rotor blade (Fig 1-13). It is likely that this occurred as a result of the impact of the aft rotor blades on the sangar structure in PB Bahadur. Oil samples were taken from all gear boxes and subsequently analysed, with no unusual findings.
Fig 1-13 Aft ‘Green’ Lag Damper Failure
Hover Meter. As the hover meter can be used as an aid to the pilots during brown out conditions, the gauges and feeding Doppler radar were sent to DSG Sealand for testing. All items tested were serviceable.
Fig 1-14 Model depicting effect of over-readingRadalt prior to impact. At impact Radalt indicated 32 ft (which would have cleared the wall – image on the left); it was actually at 22.6 ft – image on the right
Documentation. The ac’s in-use and archived paper and electronic documentation set was impounded and quarantined as part of the PCM and subsequently sent to RAF Odiham, Forward Support Wing (FSW), for formal review. The documentation set was generally found to be in good order, with all maintenance and servicing requirements correctly completed and in date. Minor administrative discrepancies were identified but would have had no effect on the ability of the ZA708 to complete tasking. The review of work carried out showed that all necessary documentation had been completed correctly, though some Serial Numbers of Work (SNOWs) (a unique ‘job number’) had been inadvertently duplicated , including some for work carried out on the Radalt. Other than the issue concerning SNOWs, which had no bearing on the accident, all other work had been recorded correctly.
Post-Accident Ac Serviceability. The report from MASU provides a detailed assessment of the damage inflicted on ZA708. It reported that the initial damage was caused by the left-hand side of the fu selage contacting a structure in flight with a subsequent aft rotor blade strike. Further, it reported that additional damage was caused to the ac structure during the expedient removal of the rotor blades and engines and the subsequent aerial recovery of ZA708 to Camp Bastion. The Panel concluded that, aside from the Radalt, ZA708 was serviceable before the accident.
Copyright Soilworks, LLC 2003-. All Rights Reserved. Soilworks®, Soiltac®,
Gorilla-Snot®, and Durasoil® are registered trademarks of Soilworks, LLC.
Copyright Soilworks, LLC 2003-. All Rights Reserved. Soilworks®, Soiltac®,
Gorilla-Snot®, and Durasoil® are registered trademarks of Soilworks, LLC.